4.9-stable review patch.  If anyone has any objections, please let me know.

------------------

From: Tony Lindgren <[email protected]>

commit 4e0f5cc65098ea32a1e77baae74215b9bd5276b1 upstream.

Otherwise the interconnect related code implementing PM runtime will
produce these errors on a failed probe:

omap_uart 48066000.serial: omap_device: omap_device_enable() called from 
invalid state 1
omap_uart 48066000.serial: use pm_runtime_put_sync_suspend() in driver?

Note that we now also need to check for priv in omap8250_runtime_suspend()
as it has not yet been registered if probe fails. And we need to use
pm_runtime_put_sync() to properly idle the device like we already do
in omap8250_remove().

Fixes: 61929cf0169d ("tty: serial: Add 8250-core based omap driver")
Signed-off-by: Tony Lindgren <[email protected]>
Signed-off-by: Greg Kroah-Hartman <[email protected]>

---
 drivers/tty/serial/8250/8250_omap.c |    8 +++++++-
 1 file changed, 7 insertions(+), 1 deletion(-)

--- a/drivers/tty/serial/8250/8250_omap.c
+++ b/drivers/tty/serial/8250/8250_omap.c
@@ -1237,7 +1237,8 @@ static int omap8250_probe(struct platfor
        pm_runtime_put_autosuspend(&pdev->dev);
        return 0;
 err:
-       pm_runtime_put(&pdev->dev);
+       pm_runtime_dont_use_autosuspend(&pdev->dev);
+       pm_runtime_put_sync(&pdev->dev);
        pm_runtime_disable(&pdev->dev);
        return ret;
 }
@@ -1246,6 +1247,7 @@ static int omap8250_remove(struct platfo
 {
        struct omap8250_priv *priv = platform_get_drvdata(pdev);
 
+       pm_runtime_dont_use_autosuspend(&pdev->dev);
        pm_runtime_put_sync(&pdev->dev);
        pm_runtime_disable(&pdev->dev);
        serial8250_unregister_port(priv->line);
@@ -1345,6 +1347,10 @@ static int omap8250_runtime_suspend(stru
        struct omap8250_priv *priv = dev_get_drvdata(dev);
        struct uart_8250_port *up;
 
+       /* In case runtime-pm tries this before we are setup */
+       if (!priv)
+               return 0;
+
        up = serial8250_get_port(priv->line);
        /*
         * When using 'no_console_suspend', the console UART must not be


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