Official Story on Top, Real Story at the bottom ...
===================

SEA02FA060NTSB Identification: SEA02FA060 Accident occurred Thursday, March 
28, 2002 at Seattle, WA Aircraft: Boeing S-307, registration: N19903 
Injuries: 4 Uninjured. This is preliminary information, subject to change, 
and may contain errors. Any errors in this report will be corrected when 
the final report has been completed.

On March 28,2002, approximately 1305 Pacific standard time, a Boeing S-307 
Stratoliner, N19903, registered to the National Air &Space Museum, operated 
by The Boeing Company, as a 14 CFR Part 91 maintenance and proficiency 
flight, ditched in the waters of Elliott Bay, Seattle, Washington, 
following a loss of engine power. Visual meteorological conditions 
prevailed at the time and no flight plan was filed. The aircraft was 
substantially damaged. The two airline transport pilots and two flight 
engineers were not injured.

The flight departed from Everett, Washington, and was destined for Seattle, 
Washington. During an interview, the flight crew reported that the purpose 
of the flight was for maintenance/systems checks and crew proficiency. The 
flight departed from Boeing Field (BFI), Seattle, approximately 1230 en 
route to Everett, Paine Field (PAE). The Captain reported that he made a 
full stop landing at PAE without incident. The aircraft was taxied back to 
the runway and the takeoff was initiated.

Shortly after lift-off, the number three engine experienced a momentary 
surge, then normalized. Due to this anomaly, the flight crew decided to 
discontinue the flight activities and return to BFI. In preparation for 
landing at BFI, the landing gear was lowered, however, the left main gear 
did not fully extend. The approach was aborted to orbit the area to try and 
remedy the situation.

The Captain reported that the flight engineer at the radio station, left 
his station to try and manually hand-crank the left gear down. After a few 
minutes, the flight crew reported a green (fully extended) light for the 
left main. The flight then headed back to BFI when a low fuel pressure 
light was noted for the number three engine followed by a loss of power.

The flight crew feathered the engine when low fuel pressure was noted to 
the remaining three engines which all subsequently began to lose power. The 
Captain reported that he did not believe that the aircraft could make it 
safely to BFI and opted to ditch the aircraft in Elliott Bay near the 
shoreline.

The aircraft impacted the water in a slightly right wing low, level 
attitude and remained upright. The aircraft remained afloat and all four 
flight crew members safely exited the aircraft and were rescue within 
minutes of the accident.

==============

And now for the REST of the story........

I just talked to Jerry Janes today, who himself just finished talking to 
his "mole" at Boeing... Someone in the maintenance department, who was in 
on the Boeing interview of the pilots afterwards... The story is that these 
highly trained Boeing test pilots decided they'd take this airplane out for 
a flight, to do some circuits. They were paying for it themselves, out of 
their own pockets, so elected to only put *300 gallons* of gas in it when 
they were on the ground at Boeing Field. They were hoping to avoid Galvin 
Flying's extra $0.04/gallon by putting more in when they got to Paine Field 
(where gas was cheaper) to do circuits.

Somewhere enroute to Paine Field, the fuel situation was driven from their 
mind, probably because they were having so much fun flying.....so they did 
circuits at Paine until the #3 engine coughed, then died. They feathered 
the prop, and decided they should probably land to investigate.

They selected gear down, to find that the gear leg under the #3 engine 
wouldn't lower, because the hydraulic pump needed to do that was powered by 
the #3 engine (now feathered). So they lowered the gear leg manually, but 
decided (get this) to fly *back to Boeing Field* to park the plane, rather 
than land at Paine Field. Shortly after making that bright decision, the 
other engines started failing. No engines were running by the time it 
ditched, and three of the four props weren't feathered.

The kicker here:The Stratoliner's maintenance base is apparently *at Paine 
Field*. Any maintenance to be done would require that it be brought back to 
Paine Field anyway (or a bunch of equipment moved to Boeing Field). When 
asked why they wanted to bring it back to Boeing Field, the response was 
"Well, our cars were at Boeing Field". Someone should have asked where 
their *boats* were.

A detail that may be useful, if you're keeping track in your head: 
According to Jerry, these engines, at 30" manifold and 2000 rpm, would burn 
about 50 gal/hr each in cruise, and would average more like 70-80 gal/hr 
each if you were doing circuits. Some things that weren't reported in the 
article below: When they peeled back the interior linings, they found that 
"it's all twisted at the bulkhead where the spar attaches to the fuselage" 
(Jerry's words). I didn't think to ask whether Jerry meant that the spar is 
twisted, the bulkhead is twisted, or what. Jerry said that both main gear 
legs were both ripped off by the ditching, and were found floating next to 
the aircraft... I thought I saw one hanging from the engine in the photos 
that Mark sent the link to, but I could be wrong.

The official explanation to date is that the engines failed due to "air in 
the fuel lines". I guess that's one way of putting it. My take is that the 
dipsticks were in the cockpit, and not in the fuel tanks."
_______________________
Scott MacLean
[EMAIL PROTECTED]
ICQ: 9184011
http://www.nerosoft.com

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