Well, the $9 repair of my rear SLS leak is provisionally successful.
The story:

I jacked up the back of the car, high as I could get it.  Two jacks,
two jackstands.  I sprayed PB Blaster on all the hydraulic fittings.
The height valve may have been messed with, the locknut isn't anywhere
near the socket on one end.  Looks to me like the shaft seal on the
left cylinder is blown.  Won't know for sure until I get it out.  Need
to do some reading, next.

I opened up the trunk to dry out, water had gotten in.

I did some reading, so I felt qualified to remove the rear seat.
(This is harder on a car with the reclining rear seat option, I've
done plenty of the others.  The manual wasn't very helpful at all.)
First remove the two 10mm bolt heads visible along the seat bottom,
near where the release clips are on a non-recliner.  That lets the
seat bottom lift up and out, and you have to unplug the heating
elements along the way.  (Unplug the backs, too.)  The seat back was
trickier.  Remove the _three_ 10mm bolts that are tucked under the
seat back, one of them in the center underneath the plastic shield for
the recliner motor, and _not_ the two visible ones that are attached
to the geared track.  That lets you lift up on the seat back,
releasing the upper posts from the holes in the reclining rack.  Then
the seat back comes out of the car.  _Now_ remove the two 10mm bolts
holding the reclining back frame to the geared tracks, and flip the
frame up enough to allow the sound padding to be pulled back.  This
exposes the area where the two plastic body plugs have to be removed,
but first you might have to unclip the radio amplifier and the seat
heater relay to get them out of the way.  Once everything is out of
the way the two plastic body plugs may be pried out, exposing the
hydraulic strut connections.

I got the control link removed from the valve.  To grip the flats on
the ball I needed a thin 8-9mm wrench , which I didn't really have,
but I made do with the prybar I'd made for the 380 SL trunk hinge pin
operation.  It gripped well enough somehow to crack loose the nut.
That and a 10mm wrench and I got the link loose from the valve's
control arm.  I then had room enough to swing the 11mm wrench on the
bleed screw.  The valve body wanted to twist on its sheet-metal mount,
so I used an 18" Crescent-style wrench to put a hold on it.  I had the
piece of tubing I use for bleeding clutch slave cylinders on the
nipple, with the other end in a clean ATF bottle.  Rather than the 1/2
liter that _should_ come out, I got maybe half of the tubing filled.
Yeah, the system was empty all right!

Anyway, a 17mm offset box wrench cracked loose the hydraulic fitting.
I removed the two washers and the banjo fitting and wrapped the open
bits with aluminum foil to keep out dirt.  I got the two 17mm bolts on
the bottom removed, but the 17mm nut on top didn't want to crack
loose.  I should have tried the penetrant first, because I managed to
badly twist the 8mm flat that's on the top of the strut.  Oops!  I put
penetrant on and left it to soak.  A little red heat would cure the
problem, but applying said heat would be unwise as the gas tank is
right next to the nut.

After a couple of hours of soaking I got out a rubber mallet and a
stick of wood.  I wedged the wood through the keyhole shaped body hole
and spun the strut with the wrench until the hydraulic fitting wedged
up against the wood.  I then put the vise grips on the twisted flat on
top the strut and struck the wrench with the mallet.  Between the
penetrant and the shock transmitted against the vise grips and the
stick the nut popped loose.  It was then a simple matter to raise the
tire a bit with the jack, to release the tension on the strut and then
remove it bodily from the car.  The strut seemed to be in very good
shape, apart from the leaking.  MB P/N 126 320 46 13, Sachs P/N 012400
102 178 R.J  (According to the EPC, this is used in 1988+ cars.)  The
ruined accordion boot looks like MB P/N 448 006 10 0?, the last digit
(and a half, really) is obscured by a vent hole.  This part number
doesn't seem to be in the EPC.  There's also a 53932 and a 1-2 molded
into it, and a mystery logo that looks a bit like a hand giving the
'OK' sign.

I cleaned it off some and pulled back the damaged accordion boot.  I
could see a circular snap ring inside the strut body, so I got out a
bar clamp and used it between the protruding shoulder of the plug and
the shoulder at the top of the strut.  Modest pressure caused the plug
to push in fractionally, releasing the tension on the snap ring.
Unfortunately I was out of time to proceed further.  It is clear that
this strut isn't much like the one I found the rebuild article on.

A little digging with some small screwdrivers got the snap ring out of
the strut, whereupon the end sealing plug could be pulled out.  There
was a second snap ring inside that kept in the piston, that came out
much the same.  The piston itself has what looks like an engine
compression ring, and it seems there may be some fine holes covered
with spring washers in it.  (I could see how the damping might be set
by this.)  No way the piston could be considered fluid-tight.  The
difficult part was removing the ball-joint end from the piston's rod.
I found a couple of flatter than normal wrenches.  One of them, an
Indian 5/8", I ground flatter and opened up the jaws a bit to fit the
thin flat on the piston rod.  The 3/4" fit as-is on the ball joint
end.  A bit of banging on the wrenches on the anvil cracked loose the
threads, then I could just unscrew the ball joint.  With that off the
rubber accordion boot and the sealing plug slid right off the end.
The sealing plug has a fat O-ring on the outside, which I don't think
was leaking, and a blue plastic seal ring backed up with a rubber
O-ring on the inside.  The two rings are kept in place by a staked-in
cup.  I don't know how one would find replacements for these seals.
I'm going to try calling hydraulic rebuild houses in town.

The ball joint feels good, and its boot is good too.  Only the
accordion boot and the rod seal appear to be bad.

Seems to me that the auxiliary spring pressure of the strut is set by
the diameter of the _rod_ versus the pressure in the strut, and that
the amount of damping is determined by the larger piston diameter (and
the size of the valved leak holes in it) as it plunges back and forth
through the fluid that fills the cylinder.  (A lesser amount of
damping is due to the smaller amount of fluid flowing to the
accumulator spheres on compression.  [Determined by the rod size.]
The ratio of the piston to rod size no doubt sets one of the
characteristics of the suspension.)  The seal plug is responsible for
keeping in all the fluid, of course, sealing the piston rod against
the pressure inside the strut.  It's a rather elegant design.

I called around town to hydraulic shops, and most didn't want anything
to do with it.  The gal at American Seal Company, an affiliate of
American West Chrome, said to bring it in and they'd have a look at
it.  They weren't too sanguine initially, but once I picked the seals
out of the plug things started looking up.  They looked pretty normal
to her and she got out the calipers for a bit of measurement and then
ran upstairs.  When she came back down she said that I should buy a
lottery ticket today!  She plopped a seal on the counter that looked
just like what I'd pulled out, except that the plastic was brown.  The
two parts I bought were this MKR-22X29.5X3 Metric Buffer (Date code
12/21/06, SKU 146886), at $7.36, and a MOR38X4 Metric O-Ring for the
outside of the plug, at $0.80.  The total bill came to $8.87, a far
cry from the pushing $400 that a new strut would run to.  It remains
to be seen, however, whether I can get it back together in a leak-free
state.  The big problem is the hard plastic pressure seal, which I
believe went in before the pieces of the plug were staked together.
Perhaps if I heat the ring in boiling water it'll be soft enough to
put in place the same way I took the old one out, but without
deforming in any permanent way.  She said that if I ruined that one
another was more than a week away, as the one I bought was the last
one on the shelf.

I also hear that activesuspensionsystems.com might rebuild these
struts.  (Probably not.)

Reading indicates that the steep interior slope of the buffer ring
should face inwards, and that customarily such seals are used in
conjunction with a secondary seal afterwards.  (Fluid that gets past
the buffer seal is captured by the secondary seal, and pumped back
into the cylinder past the shallow slope of the buffer ring on its
return stroke.)  Well, there is no such seal here.  There is also
customarily a wiper seal at the outside to keep out grit, but I
suppose that an intact accordion boot takes the place of that.  The
same source indicates that heating the ring in hot (150 degrees F)
water is appropriate to soften it for ease of installation.

Pan of hot water ready, I heated the plug (a bit) and the old seal.
The plan was to push the seal into the plug from the narrow piston
sleeve end, using a suitably-sized socket to fill the large diameter
section of the plug to try to keep the seal from going in past the
retaining lip and into the large section of the plug, in an attempt to
get the seal to seat in its channel without damage.  After practicing
a few times with the old seal to get a feel for it I installed the new
seal.  I think it went fairly well, at least it didn't look damaged or
deformed.  I then used brake cleaner to sluice everything out and then
dribbled ATF onto the sliding surfaces as an assembly lube.  I
installed the rod into the plug, then the piston into the cylinder,
and then the plug into the cylinder.  The two snap rings went in
easily.  The piston slides smoothly, but of course I won't know if
it's actually sealed until I reassemble the system and try it out.

I cleaned the accordion boot in a pan of hot TSP, which worked pretty
well, and it looks bad enough that I doubt gluing it back together
will be worth the effort.  More holes than not.  I really need a new
one.

As I'd missed my chance to call to try to order an accordion boot,
and because I could find no mention of them in the online parts
ordering systems or my copy of the EPC, I began gluing up this one.
Shoe Goo, of course.  If I can't get another boot this'll be better
than nothing.

I called Rusty, and the boot is not separately available.
More gluing, I guess...

It might be possible to find something from a place like Gardan Mfg.,
but their off-the-shelf selection didn't look that promising.  The
boot needs an extension range of 1.75"-6.5" (overall length), an
outside diameter of no more than 2.25", and a clamping flange of 1.5"
on one end, and 7/8" on the other.

I contacted them with these specifications, and they quoted $72 each.
Too rich for my blood, I think.

I reassembled the strut.  The hard part was, of course, getting the
repaired but still fragile rubber boot installed with its retaining
spring circlips.  Eventually I prevailed.  I then installed the strut
in the car.  That was easy, especially when compared with getting it
out!  I heated the copper hydraulic sealing washers red-hot and
quenched them in water, thus annealing (softening) them, and attached
the hydraulic hose.  I put a quart of the special hydraulic fluid in
the tank and started the engine, and manipulated the leveling valve.
When I next looked the tank was empty, so I put in the second quart.
The car then started going up and down with the valve.  No sign of
leaks.  I reattached the control link to the valve and took the car
for a drive.  It worked fine, except that I'd forgotten that we didn't
have snow tires and I managed to put us into a ditch!  A kindly
neighbor pulled us out.  Once home again I put the snow tires on,
cleaned up the work area, and put the car away.  Still no sign of
leaks.  I need to put the rear seat back next.

-- Jim



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