Today's log: Ah _there_ it is! The idle controller, though behind the glovebox as advertised, is tucked to the left sideways against the HVAC plenum and _not_ forward against the firewall as shown in the manual. (Those are the blower and temperature controllers for the ACC system, and the fuel pump relay.) It's marked:
002 545 33 32 Leerlaufdrehzahrlregelung Idle Speed Control 8Zyl. 412.202/010 12V It is, I might add, a VDO unit and not Bosch. I've come to expect soldering trouble from VDO's electronics, whereas Bosch's don't seem to have nearly as much trouble. Opened, it revealed a LM2901 quad comparitor, two LM2902 quad op-amps, three signal transistors, one power transistor, sixteen diodes, six electrolytic capacitors, and the usual handful of resistors and capacitors. Two of the resistors were mounted on stakes and looked like tuneable items. (Idle speed being one, I presume.) This circuit was also varnish-coated, so I hit it with the paint stripper too. The soldering didn't really look that bad, but it doesn't take all that long to redo. There were a few spots that looked questionable. I also pulled the monovalve and had a look at it. It looked good, the diaphragm was not torn. I cleaned the screen off with a bristle brush and put it back together. The coil continuity was good, the plunger was not hydrolocked. The stupid hood pad fell down again, so I had to glue it back up. What a pain! The car started easily, and idled normally. We'll see how it behaves. ...Some have suggested I check into Remco's towing products. They have a driveshaft disconnector, and a transmission lube pump system! (As well as tow bars, etc.) That lube pump system looks very interesting, I bet one of them can be adapted to this car even if they don't officially offer it. Driving the car today the idle seemed as before: nothing really wrong with it. Still seems a touch high, if it bothers me enough I could try tuning the resistors inside the controller. Maybe someday. The ACC was definitely heating today, it might even have been overdoing it. On MIN it switched to cooling (vent only), so mostly it seems to be behaving itself. The foam tube kept coming off, I think it's about 1/2" too short. I'll glue on the offending end when I get home, that may have been its only problem. Once home I had some free time, so I glued on the loose end of the foam tube. I then pulled out the idle speed actuator and cleaned it out with carb cleaner. A lot of black gunk came out. Tested on the bench it seemed to behave properly, so I reinstalled it. The rubber mounting hoses are a bit loose, but I don't think they're leaking yet. They're still flexible, so I don't think I have to replace them. With the engine running a spray of carb cleaner around the valve didn't result in an RPM change, proof of sorts. I note that the vacuum advance line to the distributor is purposely disconnected, I'm going to have to go through the engine vacuum plumbing some time to put it all right. There was a missing screw on one of the exhaust manifold heat shields so I dug up a suitable 10mm screw and installed it. That should help prevent nasty rattling noises, which I hate. Next up was the AC system. I pulled off the R134a conversion fittings, there was only a residual puff of pressure. I moved the Schrader valves from the conversion fittings back to the R12 fittings, then connected up the vacuum pump and put a quick vacuum on it. It seemed to hold vacuum, so I then put about 60 psi of propane into the system, that didn't leak down either (not that I gave it much time, but I was only looking for profound leakage) and the ACC system was able to engage the compressor with that little bit of pressure. With the preliminaries out of the way I vacuumed the system for more than 1/2 hour. It took some minutes before the vacuum pump started making the rattling noise that indicates that a deep vacuum has been pulled. I don't know if there was moisture or not, but vacuuming can't hurt, and a half hour is about the minimum that'll do any real good removing moisture. Once vacuumed I then charged the sytem with the test refrigerant: 8 oz. of Isobutane/Propane (R600a/R290) mix, followed by a propane charge until the system seemed to be operating correctly. (This takes some time to sneak up on, it's not like you just put in 3 cans of R12 and call it good.) Unfortunately evening was approaching and it wasn't really all that hot, not good conditions for charging a system this way. I did see 39 degF vent temperatures, but that's no great feat under these conditions. Still, it did seem to be working. Time will tell if I have it charged right, and if the system works correctly and doesn't leak. The lights were next. I've been afraid that I might be caught in the dark with them messed up as they are. I pulled the offending bucket assembly out of the car and found that the 6-pin connector was shifted by one position, completely explaining why it wasn't working correctly. The unused pins were tarnished, suggesting that this has been wrong for more than a little time. Plugged in correctly, the lights all worked right. One fog light was still out, but I found that it was missing a spade connector inside its shell. I replaced that and then all the lights worked as they should. One of the mounting screws for the bucket assembly has a broken clip in the car's sheet metal, it doesn't grab too well but seems to work well enough. It was time to quit for the night, but I was really having trouble putting the air cleaner back on. I rerouted the offending fuel line, which cured the problem. (For the terminally curious, I have logged 34.75 hours on the car, and $27 in repair expenses.) -- Jim _______________________________________ http://www.okiebenz.com For new parts see official list sponsor: http://www.buymbparts.com/ For used parts email [EMAIL PROTECTED] To Unsubscribe or change delivery options go to: http://okiebenz.com/mailman/listinfo/mercedes_okiebenz.com