My  bilge pump and I had a small altercation this weekend. It’s a 2000 gph PAR 
unit that I have had on the boat for at least 10 years. It has never given me 
problems until it recently decided not to pump any water. The motor ran just 
fine, and I could see the water in the bilge being stirred around, but nothing 
was being sent overboard. It acted as though it had an airlock with the 
impeller only partially submerged.

I dismantled it and found that the small slit that acts as an air vent at the 
top of the plastic impeller housing  was completely plugged. This prevented any 
trapped air from escaping from the pump body. Once I cleaned the crud out of 
the vent slit, it performed as new. Good for another ten years, thank you.

Just a note to tuck away in case anyone has a similar “failure”.

Rich Knowles
INDIGO LF38
Halifax, NS.






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