This is because the gd pointer is not set early enough anymore,
such that the i2c_set_bus_num in get_board_revision can safely
execute. This results in a console hang at SPL and the boot does
not proceed.

This piece of code is anyway necessary only for really old Overo
boards with revision numbers <= 2410 and not required for the newer
boards. For these older boards, u-boot v2014.10 still works fine.

Signed-off-by: Arun Bharadwaj <a...@gumstix.com>
---
 board/overo/common.c | 14 --------------
 1 file changed, 14 deletions(-)

diff --git a/board/overo/common.c b/board/overo/common.c
index bdfa5ca..f6f6792 100644
--- a/board/overo/common.c
+++ b/board/overo/common.c
@@ -310,20 +310,6 @@ int get_board_revision(void)
 {
        int revision;
 
-#ifdef CONFIG_SYS_I2C_OMAP34XX
-       unsigned char data;
-
-       /* board revisions <= R2410 connect 4030 irq_1 to gpio112             */
-       /* these boards should return a revision number of 0                  */
-       /* the code below forces a 4030 RTC irq to ensure that gpio112 is low */
-       i2c_set_bus_num(TWL4030_I2C_BUS);
-       data = 0x01;
-       i2c_write(0x4B, 0x29, 1, &data, 1);
-       data = 0x0c;
-       i2c_write(0x4B, 0x2b, 1, &data, 1);
-       i2c_read(0x4B, 0x2a, 1, &data, 1);
-#endif
-
        if (!gpio_request(112, "") &&
            !gpio_request(113, "") &&
            !gpio_request(115, "")) {
-- 
2.1.4

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