Re: [time-nuts] HP 5328 PSU nightmare... Or stupid engineer, you decide...

2009-09-11 Thread Steve Rooke
Hi Douglas,

I have no experience with this beast but to draw this sort of current
it points to a possible bypass cap short. If there are any dipped
tants in there, there is a high possibility that one or more of them
have gone short. If you have a good 4-wire ohm meter and a kelvin
probe, just check round to see if you can find some that are very low
ohms before you end up un-soldering them. Other than that it's down to
un-soldering off parts of the circuit to see where the big load is.
Logical isolation always seems the most sensible way to isolate
circuits but the number of time this has let me down so I frequently
use a binary chop method and make no 'educated guesses'. A variac
works well to drop the voltage but you may not easily find the fault
on a a switcher this way. At the very least you will always need good
ways to un-solder things.

I'm sure we will all look forward to your input to the group and it
will be interesting to hear in what field of time-nuttiness you work.

Regards,
Steve

2009/9/10 Douglas Wire - PUPCo Studios cont...@pupcostudios.com:
 Good day everyone and thank you all for hosting this wonderful community
 and allowing me to participate. I have several HP5328 with the “really-
 nice” newer 10811-x Oscillators in them. I have found while I have
 used the good old gold trace reliable HP instruments all of my life, these
 units have been especially difficult. The first unit the 4500uF
 electrolytic’s went bad and produced essentially a dead short; an easy
 enough repair for me to not only track down in minutes, but it only takes a
 straight bit screwdriver to fix in seconds!



 Now our second unit has been giving me fits and while I would agree 100%
 with one of the posts I saw here about how well HP did not only with their
 schematics, but also the wonderful troubleshooting flow charts usually make
 repairs on any of their old units a breeze. Sadly I have a unit here that
 is giving us fits! It is a PSU issue and not related to the Motherboard or
 any of the cards as I tested it with everything unhooked/ unsoldered and
 still got the same result. It is quite similar to what we see when we get
 an old HP unit that has a fried cap and is darn near creating a short to
 ground, but alas I simply cannot find the problem (I am sure it is starring
 me in the face is and I just can’t see it…) What I am seeing is super
 high current flow through the R1 (I believe, but HP’s every unit I have
 ever serviced had.47Ω resistor, NOT a 22-Ω as is stated in the
 schematic…) that leads to F1. The troubleshooting is complicated by the
 fact that unless I want to smoke that heavy duty, relatively close
 tolerance resistor, I cannot even check voltages anywhere for it will blow
 the fuse or if I put a slow blow to try and catch some measurements in a
 second or two, well that is not very feasible either.



 If I had to guess, I would say it has either a cap that has fried, outside
 chance of a transformer issue, or the way this thing reacts, pretty well an
 effective dead short somewhere, but I will be damned if I can find the
 problem anywhere. I replaced the bad and 4500uF caps as well as the
 rectifier, wondering if part of it had blown with no change in its issues.
 One cannot follow the flow cart to much of anything other than boxes that
 say look for a short, but so many areas one tests even on a perfectly
 working unit come clear down near the zero Ω point even when they are
 operating correctly.



 I apologize if 1) this is not a clear email that anyone can easily
 understand and 2) I almost feel embarrassed to ask anyone for advice from
 their practical experience, for I feel as If I should easily be able to get
 to the bottom of this in a matter of minutes with the wonderful data HP
 provides us all for these old workhorses.



 So if anyone has run into a problem such as this in the past where working
 the flow chart only yields No, No, No - check for shorts and has any
 advice for how I might logically proceed, or what in fact you have found
 out in dealing with a similar problem, it would be of great help, as we
 need this in-service ASAP, but I guess I just cannot see the forest for the
 tress in front of me or something here… Any advise, suggestions would be
 greatly appreciated.



 I would like to become a more active participant here with all I can
 contribute, which hopefully soon should be a lot as I am doing some
 innovative timing and generation processes that I am relatively sure the
 outcome and data from derived from it could be of great benefit to the TIME-
 NUTS userbase here. Thanks and don’t be too hard on me for asking (what to
 me sounds like a stupid amateur question) but I am either too tired to
 reason correctly, or it is just one of those very pesky problems, that
 hopefully someone has identified before and might be able to enlighten us
 over. I am begiinign to wonder if a voltage regulator might be responsible,
 but I am at a loss at the moment and have 

Re: [time-nuts] HP 5328 PSU nightmare... Or stupid engineer, you decide...

2009-09-09 Thread Adrian
Douglas,

there are lots of folks out there that are much more familiar with the
5328A, but here is what I think about it at a first glance.

If F1 blows quickly, there is a serious overload / short situation.
Don't try fixing by swapping fuses.

If you can't measure a short (that would be the first thing to look
for), THEN you might have luck checking the overvoltage protection circuit.

It consists of power Z-diode CR11. Chances are the +15 volts are out of
spec (probably due to a faulty regulator circuit), so the 17V diode
shorts the voltage and lets F1 blow.

You can unsolder CR11 to see if that is what happens. However,
disconnect everything from the +15 volts before you switch on again.
Otherwise you risk serious damage to other circuitry.

Hope that helps.

Good luck!

Adrian


Douglas Wire - PUPCo Studios schrieb:
 Good day everyone and thank you all for hosting this wonderful community
 and allowing me to participate. I have several HP5328 with the “really-
 nice” newer 10811-x Oscillators in them. I have found while I have
 used the good old gold trace reliable HP instruments all of my life, these
 units have been especially difficult. The first unit the 4500uF
 electrolytic’s went bad and produced essentially a dead short; an easy
 enough repair for me to not only track down in minutes, but it only takes a
 straight bit screwdriver to fix in seconds!

  

 Now our second unit has been giving me fits and while I would agree 100%
 with one of the posts I saw here about how well HP did not only with their
 schematics, but also the wonderful troubleshooting flow charts usually make
 repairs on any of their old units a breeze. Sadly I have a unit here that
 is giving us fits! It is a PSU issue and not related to the Motherboard or
 any of the cards as I tested it with everything unhooked/ unsoldered and
 still got the same result. It is quite similar to what we see when we get
 an old HP unit that has a fried cap and is darn near creating a short to
 ground, but alas I simply cannot find the problem (I am sure it is starring
 me in the face is and I just can’t see it…) What I am seeing is super
 high current flow through the R1 (I believe, but HP’s every unit I have
 ever serviced had.47Ω resistor, NOT a 22-Ω as is stated in the
 schematic…) that leads to F1. The troubleshooting is complicated by the
 fact that unless I want to smoke that heavy duty, relatively close
 tolerance resistor, I cannot even check voltages anywhere for it will blow
 the fuse or if I put a slow blow to try and catch some measurements in a
 second or two, well that is not very feasible either.

  

 If I had to guess, I would say it has either a cap that has fried, outside
 chance of a transformer issue, or the way this thing reacts, pretty well an
 effective dead short somewhere, but I will be damned if I can find the
 problem anywhere. I replaced the bad and 4500uF caps as well as the
 rectifier, wondering if part of it had blown with no change in its issues.
 One cannot follow the flow cart to much of anything other than boxes that
 say look for a short, but so many areas one tests even on a perfectly
 working unit come clear down near the zero Ω point even when they are
 operating correctly.

  

 I apologize if 1) this is not a clear email that anyone can easily
 understand and 2) I almost feel embarrassed to ask anyone for advice from
 their practical experience, for I feel as If I should easily be able to get
 to the bottom of this in a matter of minutes with the wonderful data HP
 provides us all for these old workhorses.

  

 So if anyone has run into a problem such as this in the past where working
 the flow chart only yields No, No, No - check for shorts and has any
 advice for how I might logically proceed, or what in fact you have found
 out in dealing with a similar problem, it would be of great help, as we
 need this in-service ASAP, but I guess I just cannot see the forest for the
 tress in front of me or something here… Any advise, suggestions would be
 greatly appreciated.

  

 I would like to become a more active participant here with all I can
 contribute, which hopefully soon should be a lot as I am doing some
 innovative timing and generation processes that I am relatively sure the
 outcome and data from derived from it could be of great benefit to the TIME-
 NUTS userbase here. Thanks and don’t be too hard on me for asking (what to
 me sounds like a stupid amateur question) but I am either too tired to
 reason correctly, or it is just one of those very pesky problems, that
 hopefully someone has identified before and might be able to enlighten us
 over. I am begiinign to wonder if a voltage regulator might be responsible,
 but I am at a loss at the moment and have not had enough sleep to properly
 think this repair through… Thank you again everyone!

  

 Warm regards,

 Douglas M. Wire, GED, FNA,

 PUPCo Studios, PUPCo Research Group

  

  

 ___
 

Re: [time-nuts] HP 5328 PSU nightmare... Or stupid engineer, you decide...

2009-09-09 Thread Brent Gordon
I'm not familiar with this particular instrument, but a standard
technique for linear power supplies is to hook it up to a variac. This
lets you turn down the line voltage so you can do some measurements
without smoking the system.

Brent

Douglas Wire - PUPCo Studios wrote:
 Good day everyone and thank you all for hosting this wonderful community
 and allowing me to participate. I have several HP5328 with the “really-
 nice” newer 10811-x Oscillators in them. I have found while I have
 used the good old gold trace reliable HP instruments all of my life, these
 units have been especially difficult. The first unit the 4500uF
 electrolytic’s went bad and produced essentially a dead short; an easy
 enough repair for me to not only track down in minutes, but it only takes a
 straight bit screwdriver to fix in seconds!

  

 Now our second unit has been giving me fits and while I would agree 100%
 with one of the posts I saw here about how well HP did not only with their
 schematics, but also the wonderful troubleshooting flow charts usually make
 repairs on any of their old units a breeze. Sadly I have a unit here that
 is giving us fits! It is a PSU issue and not related to the Motherboard or
 any of the cards as I tested it with everything unhooked/ unsoldered and
 still got the same result. It is quite similar to what we see when we get
 an old HP unit that has a fried cap and is darn near creating a short to
 ground, but alas I simply cannot find the problem (I am sure it is starring
 me in the face is and I just can’t see it…) What I am seeing is super
 high current flow through the R1 (I believe, but HP’s every unit I have
 ever serviced had.47Ω resistor, NOT a 22-Ω as is stated in the
 schematic…) that leads to F1. The troubleshooting is complicated by the
 fact that unless I want to smoke that heavy duty, relatively close
 tolerance resistor, I cannot even check voltages anywhere for it will blow
 the fuse or if I put a slow blow to try and catch some measurements in a
 second or two, well that is not very feasible either.

  

 If I had to guess, I would say it has either a cap that has fried, outside
 chance of a transformer issue, or the way this thing reacts, pretty well an
 effective dead short somewhere, but I will be damned if I can find the
 problem anywhere. I replaced the bad and 4500uF caps as well as the
 rectifier, wondering if part of it had blown with no change in its issues.
 One cannot follow the flow cart to much of anything other than boxes that
 say look for a short, but so many areas one tests even on a perfectly
 working unit come clear down near the zero Ω point even when they are
 operating correctly.

  

 I apologize if 1) this is not a clear email that anyone can easily
 understand and 2) I almost feel embarrassed to ask anyone for advice from
 their practical experience, for I feel as If I should easily be able to get
 to the bottom of this in a matter of minutes with the wonderful data HP
 provides us all for these old workhorses.

  

 So if anyone has run into a problem such as this in the past where working
 the flow chart only yields No, No, No - check for shorts and has any
 advice for how I might logically proceed, or what in fact you have found
 out in dealing with a similar problem, it would be of great help, as we
 need this in-service ASAP, but I guess I just cannot see the forest for the
 tress in front of me or something here… Any advise, suggestions would be
 greatly appreciated.

  

 I would like to become a more active participant here with all I can
 contribute, which hopefully soon should be a lot as I am doing some
 innovative timing and generation processes that I am relatively sure the
 outcome and data from derived from it could be of great benefit to the TIME-
 NUTS userbase here. Thanks and don’t be too hard on me for asking (what to
 me sounds like a stupid amateur question) but I am either too tired to
 reason correctly, or it is just one of those very pesky problems, that
 hopefully someone has identified before and might be able to enlighten us
 over. I am begiinign to wonder if a voltage regulator might be responsible,
 but I am at a loss at the moment and have not had enough sleep to properly
 think this repair through… Thank you again everyone!

  

 Warm regards,

 Douglas M. Wire, GED, FNA,

 PUPCo Studios, PUPCo Research Group

   

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Re: [time-nuts] HP 5328 PSU nightmare... Or stupid engineer, you decide...

2009-09-09 Thread Bruce Griffiths
Neither the linear regulators nor the switching regulators in the 5328A have
any explicit current limiting circuitry other than that provided by the
pass transistor current gain and the limited current available from the
pass element driver.

The only protection against long term load faults is provided by the fuses
at the regulator inputs. However these fuses don't protect against
shorted rectifier output filter capacitors etc.

Bruce

Brent Gordon wrote:
 I'm not familiar with this particular instrument, but a standard
 technique for linear power supplies is to hook it up to a variac. This
 lets you turn down the line voltage so you can do some measurements
 without smoking the system.

 Brent

 Douglas Wire - PUPCo Studios wrote:
   
 Good day everyone and thank you all for hosting this wonderful community
 and allowing me to participate. I have several HP5328 with the “really-
 nice” newer 10811-x Oscillators in them. I have found while I have
 used the good old gold trace reliable HP instruments all of my life, these
 units have been especially difficult. The first unit the 4500uF
 electrolytic’s went bad and produced essentially a dead short; an easy
 enough repair for me to not only track down in minutes, but it only takes a
 straight bit screwdriver to fix in seconds!

  

 Now our second unit has been giving me fits and while I would agree 100%
 with one of the posts I saw here about how well HP did not only with their
 schematics, but also the wonderful troubleshooting flow charts usually make
 repairs on any of their old units a breeze. Sadly I have a unit here that
 is giving us fits! It is a PSU issue and not related to the Motherboard or
 any of the cards as I tested it with everything unhooked/ unsoldered and
 still got the same result. It is quite similar to what we see when we get
 an old HP unit that has a fried cap and is darn near creating a short to
 ground, but alas I simply cannot find the problem (I am sure it is starring
 me in the face is and I just can’t see it…) What I am seeing is super
 high current flow through the R1 (I believe, but HP’s every unit I have
 ever serviced had.47Ω resistor, NOT a 22-Ω as is stated in the
 schematic…) that leads to F1. The troubleshooting is complicated by the
 fact that unless I want to smoke that heavy duty, relatively close
 tolerance resistor, I cannot even check voltages anywhere for it will blow
 the fuse or if I put a slow blow to try and catch some measurements in a
 second or two, well that is not very feasible either.

  

 If I had to guess, I would say it has either a cap that has fried, outside
 chance of a transformer issue, or the way this thing reacts, pretty well an
 effective dead short somewhere, but I will be damned if I can find the
 problem anywhere. I replaced the bad and 4500uF caps as well as the
 rectifier, wondering if part of it had blown with no change in its issues.
 One cannot follow the flow cart to much of anything other than boxes that
 say look for a short, but so many areas one tests even on a perfectly
 working unit come clear down near the zero Ω point even when they are
 operating correctly.

  

 I apologize if 1) this is not a clear email that anyone can easily
 understand and 2) I almost feel embarrassed to ask anyone for advice from
 their practical experience, for I feel as If I should easily be able to get
 to the bottom of this in a matter of minutes with the wonderful data HP
 provides us all for these old workhorses.

  

 So if anyone has run into a problem such as this in the past where working
 the flow chart only yields No, No, No - check for shorts and has any
 advice for how I might logically proceed, or what in fact you have found
 out in dealing with a similar problem, it would be of great help, as we
 need this in-service ASAP, but I guess I just cannot see the forest for the
 tress in front of me or something here… Any advise, suggestions would be
 greatly appreciated.

  

 I would like to become a more active participant here with all I can
 contribute, which hopefully soon should be a lot as I am doing some
 innovative timing and generation processes that I am relatively sure the
 outcome and data from derived from it could be of great benefit to the TIME-
 NUTS userbase here. Thanks and don’t be too hard on me for asking (what to
 me sounds like a stupid amateur question) but I am either too tired to
 reason correctly, or it is just one of those very pesky problems, that
 hopefully someone has identified before and might be able to enlighten us
 over. I am begiinign to wonder if a voltage regulator might be responsible,
 but I am at a loss at the moment and have not had enough sleep to properly
 think this repair through… Thank you again everyone!

  

 Warm regards,

 Douglas M. Wire, GED, FNA,

 PUPCo Studios, PUPCo Research Group

   
 

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Re: [time-nuts] HP 5328 PSU nightmare... Or stupid engineer, you decide...

2009-09-09 Thread Dave M


I'm not familiar with this particular instrument, but a standard
technique for linear power supplies is to hook it up to a variac. This
lets you turn down the line voltage so you can do some measurements
without smoking the system.

Brent

Douglas Wire - PUPCo Studios wrote:

Good day everyone and thank you all for hosting this wonderful community
and allowing me to participate. I have several HP5328 with the ?really-
nice? newer 10811-x Oscillators in them. I have found while I have
used the good old gold trace reliable HP instruments all of my life, 
these

units have been especially difficult. The first unit the 4500uF
electrolytic?s went bad and produced essentially a dead short; an easy
enough repair for me to not only track down in minutes, but it only takes 
a

straight bit screwdriver to fix in seconds!



Now our second unit has been giving me fits and while I would agree 100%
with one of the posts I saw here about how well HP did not only with 
their
schematics, but also the wonderful troubleshooting flow charts usually 
make

repairs on any of their old units a breeze. Sadly I have a unit here that
is giving us fits! It is a PSU issue and not related to the Motherboard 
or

any of the cards as I tested it with everything unhooked/ unsoldered and
still got the same result. It is quite similar to what we see when we get
an old HP unit that has a fried cap and is darn near creating a short to
ground, but alas I simply cannot find the problem (I am sure it is 
starring

me in the face is and I just can?t see it?) What I am seeing is super
high current flow through the R1 (I believe, but HP?s every unit I have
ever serviced had.47? resistor, NOT a 22-? as is stated in the
schematic?) that leads to F1. The troubleshooting is complicated by the
fact that unless I want to smoke that heavy duty, relatively close
tolerance resistor, I cannot even check voltages anywhere for it will 
blow

the fuse or if I put a slow blow to try and catch some measurements in a
second or two, well that is not very feasible either.



If I had to guess, I would say it has either a cap that has fried, 
outside
chance of a transformer issue, or the way this thing reacts, pretty well 
an

effective dead short somewhere, but I will be damned if I can find the
problem anywhere. I replaced the bad and 4500uF caps as well as the
rectifier, wondering if part of it had blown with no change in its 
issues.

One cannot follow the flow cart to much of anything other than boxes that
say look for a short, but so many areas one tests even on a perfectly
working unit come clear down near the zero ? point even when they are
operating correctly.



I apologize if 1) this is not a clear email that anyone can easily
understand and 2) I almost feel embarrassed to ask anyone for advice from
their practical experience, for I feel as If I should easily be able to 
get

to the bottom of this in a matter of minutes with the wonderful data HP
provides us all for these old workhorses.



So if anyone has run into a problem such as this in the past where 
working

the flow chart only yields No, No, No - check for shorts and has any
advice for how I might logically proceed, or what in fact you have found
out in dealing with a similar problem, it would be of great help, as we
need this in-service ASAP, but I guess I just cannot see the forest for 
the

tress in front of me or something here? Any advise, suggestions would be
greatly appreciated.





...




Warm regards,

Douglas M. Wire, GED, FNA,

PUPCo Studios, PUPCo Research Group




Douglas,
Start by making sure that the line voltage switch is set correctly.
Barring that as a cause of the problem, you will have to start removing 
components that are fed by the +12V supply until the overcurrent is gone. 
First choice would be CR1 (12V Zener), then ICs U1, U2, U3, U4 and U5.  When 
bad component is removed, the current should drop back to normal, or 
slightly less.  That might be a lot of unsoldering, but unless you want to 
start cutting traces on the PCB, it's the only way to proceed.
If you have a good ESR meter, it can be used as a low ohms meter to locate a 
short or low resistance.
You might remove R1 and install a higher value, higher wattage resistor so 
that you avoid further damage while you make measurements.  Measure the raw 
supply voltage (+25V); make sure that it's the right voltage and low ripple.
Measure the voltage drop across R1 in an operating instrument, so that you 
have a reference of what to look for in the bad guy.  From the voltage drop, 
you can calculate the current going through  it.   Use a sensitive voltmeter 
(5 digits or better; you want to see millivolt drops along the traces) to 
trace the voltage drops along the circuit traces to find where the majority 
of the current is going.


Good luck with the troubleshooting.

Dave M
masondg44 at comcast dot net 



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Re: [time-nuts] HP 5328 PSU nightmare... Or stupid engineer, you decide...

2009-09-09 Thread Ed Palmer
Hi Dave,

I think we've all lost some hair while working on a stubborn problem.
Hang in there.

As mentioned by Brent Gordon, the Variac is your friend in situations
like this. If you don't have one, you can wire a light bulb in series
with the power cord. Use 40,60,100 watt - whatever you need. This will
limit the current so you can search for the short without blowing fuses
or letting the magic smoke out. The Variac is preferred because you may
find that everything looks good until you hit X volts. The light bulb
obviously isn't that selective.

Ed

Douglas Wire - PUPCo Studios wrote:
 Good day everyone and thank you all for hosting this wonderful community
 and allowing me to participate. I have several HP5328 with the “really-
 nice” newer 10811-x Oscillators in them. I have found while I have
 used the good old gold trace reliable HP instruments all of my life, these
 units have been especially difficult. The first unit the 4500uF
 electrolytic’s went bad and produced essentially a dead short; an easy
 enough repair for me to not only track down in minutes, but it only takes a
 straight bit screwdriver to fix in seconds!

  

 Now our second unit has been giving me fits and while I would agree 100%
 with one of the posts I saw here about how well HP did not only with their
 schematics, but also the wonderful troubleshooting flow charts usually make
 repairs on any of their old units a breeze. Sadly I have a unit here that
 is giving us fits! It is a PSU issue and not related to the Motherboard or
 any of the cards as I tested it with everything unhooked/ unsoldered and
 still got the same result. It is quite similar to what we see when we get
 an old HP unit that has a fried cap and is darn near creating a short to
 ground, but alas I simply cannot find the problem (I am sure it is starring
 me in the face is and I just can’t see it…) What I am seeing is super
 high current flow through the R1 (I believe, but HP’s every unit I have
 ever serviced had.47Ω resistor, NOT a 22-Ω as is stated in the
 schematic…) that leads to F1. The troubleshooting is complicated by the
 fact that unless I want to smoke that heavy duty, relatively close
 tolerance resistor, I cannot even check voltages anywhere for it will blow
 the fuse or if I put a slow blow to try and catch some measurements in a
 second or two, well that is not very feasible either.

  

 If I had to guess, I would say it has either a cap that has fried, outside
 chance of a transformer issue, or the way this thing reacts, pretty well an
 effective dead short somewhere, but I will be damned if I can find the
 problem anywhere. I replaced the bad and 4500uF caps as well as the
 rectifier, wondering if part of it had blown with no change in its issues.
 One cannot follow the flow cart to much of anything other than boxes that
 say look for a short, but so many areas one tests even on a perfectly
 working unit come clear down near the zero Ω point even when they are
 operating correctly.

  

 I apologize if 1) this is not a clear email that anyone can easily
 understand and 2) I almost feel embarrassed to ask anyone for advice from
 their practical experience, for I feel as If I should easily be able to get
 to the bottom of this in a matter of minutes with the wonderful data HP
 provides us all for these old workhorses.

  

 So if anyone has run into a problem such as this in the past where working
 the flow chart only yields No, No, No - check for shorts and has any
 advice for how I might logically proceed, or what in fact you have found
 out in dealing with a similar problem, it would be of great help, as we
 need this in-service ASAP, but I guess I just cannot see the forest for the
 tress in front of me or something here… Any advise, suggestions would be
 greatly appreciated.

  

 I would like to become a more active participant here with all I can
 contribute, which hopefully soon should be a lot as I am doing some
 innovative timing and generation processes that I am relatively sure the
 outcome and data from derived from it could be of great benefit to the TIME-
 NUTS userbase here. Thanks and don’t be too hard on me for asking (what to
 me sounds like a stupid amateur question) but I am either too tired to
 reason correctly, or it is just one of those very pesky problems, that
 hopefully someone has identified before and might be able to enlighten us
 over. I am begiinign to wonder if a voltage regulator might be responsible,
 but I am at a loss at the moment and have not had enough sleep to properly
 think this repair through… Thank you again everyone!

  

 Warm regards,

 Douglas M. Wire, GED, FNA,

 PUPCo Studios, PUPCo Research Group

  

  

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Re: [time-nuts] HP 5328 PSU nightmare... Or stupid engineer, you decide...

2009-09-09 Thread Hal Murray

[variac]
 If you don't have one, you can wire a light bulb in series with the
 power cord. Use 40,60,100 watt - whatever you need. 

Neat.  Thanks.  That trick wasn't on my list.

I think you can get lower wattage bulbs (at 120V).  I think I've seen 25W, 
but I'm not sure.  Old style tungsten night-lights are/were 6W.


 The Variac is preferred because you may find that everything looks
 good until you hit X volts. The light bulb obviously isn't that
 selective.

I'd expect a light bulb to work well.  If the DUT needs X volts to 
demonstrate the problem, it will act as a high resistance at low voltage and 
low resistance at high voltage.  Light bulbs are (very) non-linear in the 
other direction.  If you connect the two in series, I'd expect it to be 
stable at a balance point with some current, hopefully enough to debug things 
without burning anything out.


Here is another variation ...  I'm assuming you are chasing something like a 
short on the power rail, probably a dead bypass cap.  Things get more 
complicated if it's only sick rather than a solidly short.

If you have localized the problem to one board, power that board from a power 
supply with a current limit knob.  You may want to solder some wires onto the 
board rather than using the normal connector.

Crank the current up until you get enough voltage drop to be interesting but 
nothing is smoking.  Poke around with a volt meter.  If you have traces 
rather than a ground plane, a few amps and a reasonable meter will localize 
things.  Even with a ground plane, it will get you pretty close.


I think I remember dunking one board in a pan of Freon(?).  It was some 
liquid that bubbled at the shorted cap.  That was ~30 years ago.  Maybe I'm 
dreaming and confusing things with another story.  It does seem like a good 
approach.  Are there any good Freon like chemicals available/legal these days?



-- 
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Re: [time-nuts] HP 5328 PSU nightmare... Or stupid engineer, you decide...

2009-09-09 Thread Neville Michie

Hi,
I use a Variac routinely to turn on instruments that have been unused  
for more than a few months.
Electrolytic capacitors will often come good if slowly brought up to  
voltage.
Recently I resurrected a WW2 Command receiver that had been stored  
for 40 years.
I hooked up a power supply and set it to 10% of line voltage and  
increased it 10% at hourly intervals.
Slowly warming up the device gives the electrolytics to form up, even  
the paper capacitors get a

chance to warm and dry out a bit.
For fault finding, starting at zero volts you can watch the  
rectifiers start to take up the load, the
voltage regulators cut in when the supply reaches the regulation  
voltage and generally locate

any overloads before the smoke gets out.
The main problem is with switching regulators that abruptly cut in at  
some voltage,

a series tungsten filament lamp helps with them to avoid smoke release.
It always pays to turn it on slowly.

cheers,
Neville Michie








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Re: [time-nuts] HP 5328 PSU nightmare... Or stupid engineer, you decide...

2009-09-09 Thread Bob Martinson
As a kid I had an outlet in series with a screw-in bulb, with a switch
across it to get full voltage.  Used it very often.


73, Bob, k1REM




-Original Message-
From: time-nuts-boun...@febo.com [mailto:time-nuts-boun...@febo.com]on
Behalf Of Hal Murray
Sent: Thursday, September 10, 2009 12:50 AM
To: Discussion of precise time and frequency measurement
Subject: Re: [time-nuts] HP 5328 PSU nightmare... Or stupid engineer,
you decide...



[variac]
 If you don't have one, you can wire a light bulb in series with the
 power cord. Use 40,60,100 watt - whatever you need.

Neat.  Thanks.  That trick wasn't on my list.

I think you can get lower wattage bulbs (at 120V).  I think I've seen 25W,
but I'm not sure.  Old style tungsten night-lights are/were 6W.


 The Variac is preferred because you may find that everything looks
 good until you hit X volts. The light bulb obviously isn't that
 selective.

I'd expect a light bulb to work well.  If the DUT needs X volts to
demonstrate the problem, it will act as a high resistance at low voltage and
low resistance at high voltage.  Light bulbs are (very) non-linear in the
other direction.  If you connect the two in series, I'd expect it to be
stable at a balance point with some current, hopefully enough to debug
things
without burning anything out.


Here is another variation ...  I'm assuming you are chasing something like a
short on the power rail, probably a dead bypass cap.  Things get more
complicated if it's only sick rather than a solidly short.

If you have localized the problem to one board, power that board from a
power
supply with a current limit knob.  You may want to solder some wires onto
the
board rather than using the normal connector.

Crank the current up until you get enough voltage drop to be interesting but
nothing is smoking.  Poke around with a volt meter.  If you have traces
rather than a ground plane, a few amps and a reasonable meter will localize
things.  Even with a ground plane, it will get you pretty close.


I think I remember dunking one board in a pan of Freon(?).  It was some
liquid that bubbled at the shorted cap.  That was ~30 years ago.  Maybe I'm
dreaming and confusing things with another story.  It does seem like a good
approach.  Are there any good Freon like chemicals available/legal these
days?



--
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Checked by AVG - www.avg.com
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Re: [time-nuts] HP 5328 PSU nightmare... Or stupid engineer, you decide...

2009-09-09 Thread Ed Palmer


Hal Murray wrote:

[variac]
  

If you don't have one, you can wire a light bulb in series with the
power cord. Use 40,60,100 watt - whatever you need. 



Neat.  Thanks.  That trick wasn't on my list.

I think you can get lower wattage bulbs (at 120V).  I think I've seen 25W, 
but I'm not sure.  Old style tungsten night-lights are/were 6W.
  
Yes, and if your junk box goes back far enough, you may find some 120V 
Christmas tree bulbs!  Not sure what their wattage is.  Basically, use 
the smallest 120V (or 240V - depending on where you live) incandescent 
light bulb that gives you reasonable current / voltage in your sick 
circuit.  You can also use lower voltage bulbs on the secondary side of 
a power transformer if that works better.

The Variac is preferred because you may find that everything looks
good until you hit X volts. The light bulb obviously isn't that
selective.



I'd expect a light bulb to work well.  If the DUT needs X volts to 
demonstrate the problem, it will act as a high resistance at low voltage and 
low resistance at high voltage.  Light bulbs are (very) non-linear in the 
other direction.  If you connect the two in series, I'd expect it to be 
stable at a balance point with some current, hopefully enough to debug things 
without burning anything out.
  
True, but with the light bulb you'd miss the fact that everything looks 
good below X volts.  That could be a significant piece of info.


Here is another variation ...  I'm assuming you are chasing something like a 
short on the power rail, probably a dead bypass cap.  Things get more 
complicated if it's only sick rather than a solidly short.


If you have localized the problem to one board, power that board from a power 
supply with a current limit knob.  You may want to solder some wires onto the 
board rather than using the normal connector.


Crank the current up until you get enough voltage drop to be interesting but 
nothing is smoking.  Poke around with a volt meter.  If you have traces 
rather than a ground plane, a few amps and a reasonable meter will localize 
things.  Even with a ground plane, it will get you pretty close.


  
I've got a Jupiter GPS receiver that suddenly decided to start sucking 
silly amounts of current.  Never was able to find the short on that.  
I've got a better meter now, maybe I'll put it back on my list of things 
to fix.  Sigh.
I think I remember dunking one board in a pan of Freon(?).  It was some 
liquid that bubbled at the shorted cap.  That was ~30 years ago.  Maybe I'm 
dreaming and confusing things with another story.  It does seem like a good 
approach.  Are there any good Freon like chemicals available/legal these days?



  
Freon was nice because it was non-conductive, evaporated cleanly, and 
wasn't flammable.  I'm drawing a blank on what would be a good substitute.


Ed


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