Now, my servo motor with the attached resolver still out of the rotary
table, I have a HYOOGE success!
The cause of jerkiness was a TOO HIGH input voltage to the resolver.I am
hypothesizing that this caused too much voltage to be passed into the
resolver converter input, causing it to crowbar or o
Igor Chudov wrote:
> Now, my servo motor with the attached resolver still out of the rotary
> table, I have a HYOOGE success!
>
> The cause of jerkiness was a TOO HIGH input voltage to the resolver.I am
> hypothesizing that this caused too much voltage to be passed into the
> resolver converter inp
Congratulations,
A really nice problem/solution to be kept long and safe in the archives
of EMC-USERS!!!
Javier
On Sun, 2011-01-30 at 11:52 -0600, Jon Elson wrote:
> Igor Chudov wrote:
> > Now, my servo motor with the attached resolver still out of the rotary
> > table, I have a HYOOGE success!
On Sun, Jan 30, 2011 at 4:03 PM, jros wrote:
> Congratulations,
>
> A really nice problem/solution to be kept long and safe in the archives
> of EMC-USERS!!!
>
>
Thanks. The archives are great and searchable.
> As an SEO, I try to make sure to put all the right keywords in my articles,
> so t