Replaced the coil, wires, and plugs today with still no change. Car was
running fine before this started yesterday. I might just reboot the Link to
see if that changes anything. Gas mileage seems to be better at the moment,
but life under 5k is rather boring!

On Mon, Jul 27, 2009 at 4:47 PM, <[email protected]> wrote:

>  Sorry, I missed the part indicating the turbo wasn't on there yet.
>
> A quick guess would be the air/fuel ratio by 5K RPM.  Do you have an A/F
> gauge installed?
> Most people get "bogging" if the fuel is too high, but that could also be
> interpreted as "bucking", as the spark plugs could be getting soaked,
> causing ignition cutout.
> Have you pulled the plugs to see if you're running lean (white
> deposit/coating?)
> A dark coating would indicate you're running too rich.
> Of course, you have to put some miles on the plugs too make that judgement,
> so new plugs may not help you diagnose the problem.
>
> Now, if this is a recent problem and the larger injectors and Link have
> been working without difficulty, I'd say that you're more likely to have a
> LEAN condition, perhaps brought on by a clogging fuel filter of failing fuel
> pump.
>
>
> Jerry AKA LGO
>
> ------------------------------
>
> _______________________________________________
> Miatapower mailing list
> [email protected]
> http://list.miatapower.net/cgi-bin/mailman/listinfo/miatapower
>
>
_______________________________________________
Miatapower mailing list
[email protected]
http://list.miatapower.net/cgi-bin/mailman/listinfo/miatapower

Reply via email to