Am 16. Juni 2020 22:21:08 MESZ schrieb Vladimir Oltean <olte...@gmail.com>: >On Tue, 16 Jun 2020 at 23:10, Tom Rini <tr...@konsulko.com> wrote: >> >> On Tue, Jun 16, 2020 at 10:58:26PM +0300, Vladimir Oltean wrote: >> > Hi Tom, >> > >> > On Tue, 16 Jun 2020 at 22:55, Tom Rini <tr...@konsulko.com> wrote: >> > > >> > > Hey all, >> > > >> > > In commit 4346df3392c0 ("phy: atheros: Make RGMII Tx delays >actually >> > > configurable for AR8035") we brought in changes to get in to line >with >> > > upstream linux kernel support for this PHY and in turn deal with >more >> > > "driver was wrong, DT was wrong too" changes. Now the problem I >have is >> > > that ethernet on my Hummingboard doesn't work AND as far as I can >tell, >> > > the DTB is correct and saying phy-mode = "rgmii-id" now not >"rgmii". It >> > > also looks to match what's in v5.7 for the kernel. What do I >need to do >> > > here next? Thanks! >> > > >> > > -- >> > > Tom >> > >> > Reverting 4346df3392c0 makes your interface work? >> >> Yup. >> >> > What is the DTS path that your hummingboard uses? >> >> Good question. Per board/solidrun/mx6cuboxi/mx6cuboxi.c: >> /* >> * This is not a perfect match. Avoid dependency on the DM GPIO >driver >> * needed >> * for accurate board detection. Hummingboard2 DT is good enough for >> * U-Boot on >> * all Hummingboard/Cubox-i platforms. >> */ >> so arch/arm/dts/imx6dl-hummingboard2-emmc-som-v15.dts is the base. >But >> the board really is the original hummingboard platform. Thanks! >> >> -- >> Tom > >Does it work if you say PHY_INTERFACE_MODE_RGMII_ID here? >https://gitlab.denx.de/u-boot/u-boot/-/blob/master/drivers/net/fec_mxc.c#L1232
it should be PHY_INTERFACE_MODE_RGMII_TXID to get the original behavior, shouldn't it? The commit in question only removes the hardcoded TX delay. -michael