> Sorry, for the record I'll try to be as clear as possible. I have confirmed > the fix. When using pncconf with version 2.4.3, I needed to invert the > motor signal as determined in the open loop pncconf test. This was also > causing the MAX_OUTPUT parameter to be set to negative for that axis. > Manually changing the ini file to have a positive MAX_OUTPUT resolved the > issue. > > Thanks to all who helped resolve this. >
Glad you got it Scott and sorry PNCconf sent you down the river without a paddle - though you are using a pretty old version. one pretty painless way to use a more current version is to use the buildbot. http://buildbot.linuxcnc.org/ There you can get the latest bug fixes for your current version (2.4.7 actually not released yet) or you could checkout the soon to be released 2.5 version. Chris M ------------------------------------------------------------------------------ Get a FREE DOWNLOAD! and learn more about uberSVN rich system, user administration capabilities and model configuration. Take the hassle out of deploying and managing Subversion and the tools developers use with it. http://p.sf.net/sfu/wandisco-d2d-2 _______________________________________________ Emc-users mailing list [email protected] https://lists.sourceforge.net/lists/listinfo/emc-users
