I guess the fedex guy didn't have anything better to do, so the motor I 
ordered a couple days back walked up and splatted itself into a deck 
chair beside the front door about 10:30 ish this morning.

That meant I had just about everything on hand to convert the spindle 
drive to all metal gears, and all metal sprockets.

But it wasn't all that easy, Murphy is alive and well.

While the mounting bracket for a swing mount looked the same, it was 
welded to the field sleeve of the motor about 10mm farther from the 
flywheel.  So I had to stack up washers on the swingbolts to space it to 
align the 6 groove j pulley with its load pulley, a 3 incher.

The crescent slotted bracket to adjust belt tension, once sawed off to 
match the old one, misses backing out to align with the lock bolt by 
about 10mm, so it appears the pivot bolt holes must be 3 or 4mm farther 
from the motor body.  Its difficult to make a meaningfull measurement of 
that. So a 170mm j6 belt got ordered to replace the 160mm j6.  I hope 
that won't lay the motor too low.

I took 3.5mm off the top of the jackshaft frame so it can lift a bit 
higher in the old motor pocket under the bed, and a quick test fit seems 
to indicate that is enough rise to compensate for swapping a 10 cog XL 
sprocket out for a 16 cog XL sprocket.

On remove the old motor, it turned out that I had pinned the flywheel 
onto the shaft by drilling a hole that intersected the flywheel and the 
shaft, but I had forgotten that the tap I tried to tap the hole with, 
had broken off in the hole.  So the piece of tap is still in the hole, 
but it has wallered it out around the taps remains such that there is 
about a 2 degree looseness now. The flywheel could also be tipped on the 
shaft a degree or so, and that was what was causing it to sound as if 
the bearings on that end of the motor had turned square.

IOW the motor would be fine IF I could get the tap out, screw it back on 
tight (left hand threads too) And drill & tap a new hole, perhaps for a 
roll pin to lock it together.

This brings up a question re locking the shaft into its bearings.  Red 
threadlocker seems like it should work.  Doesn't.  Superglue seems like 
it should work.  Doesn't.  These bearings are a hundred lb or more press 
fit on this A2 shaft, and they still walk the shaft thru them given 
enough time.

So, is there a magic glue concoction that will lock the shaft to the 
bearings?

I put some red threadlocker on this flywheel and screwed the armature in 
and out several times to distribute it, then drove it on as firmly as I 
could.

My old eyes can't read the microscopic and dirty text on the threadlocker 
tube, so I don't know how long till it reaches maximum grip.  Does 
anyone know?

And despite the thread locker, should I try to drill & tap it again, only 
this time don't break the tap?

Thanks for any insight you can share everybody.

Cheers, Gene Heskett
-- 
"There are four boxes to be used in defense of liberty:
 soap, ballot, jury, and ammo. Please use in that order."
-Ed Howdershelt (Author)
Genes Web page <http://geneslinuxbox.net:6309/gene>

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