Hi again everyone
Pin No. 01 on my BOB is enable, and unless it is on HIGH the motion
commands are blocked, I've discovered that the input from the computer on
this pin is 5v (ie HIGH) but the BOB inverts this so that the output is
about 2v (ie Low) so what I now want to do is to invert the
On 5 April 2014 12:42, Bill Brettle billbret...@gmail.com wrote:
computer. There are some example on how to do this in an LCNC document
titled Stepper Configuration. (with part of that document Attached) When I
put that into my HAL file I get an error message as shown on the top line
of that
On Saturday 05 April 2014 09:28:28 Bill Brettle did opine:
Hi again everyone
Pin No. 01 on my BOB is enable, and unless it is on HIGH the motion
commands are blocked, I've discovered that the input from the computer
on this pin is 5v (ie HIGH) but the BOB inverts this so that the output
I need some clarification on lathe setup. The integrator manual seems to
indicate that I should remove the [axis_1] section. Some older posts say that I
will have to make a dummy 'y' axis.
I worked on ini/hal bugs/learning curve until I got Axis to appear without
crashing setup just as a
Thankyou both
First, the LOW on pin 1 was 0v sorry to muddy the waters.
Second, I corrected the -out-invert problem now I get this Error message
Debug file information:
Can not find -sec MOT -var MOT -num 1
Can not find -sec IO -var IO -num 1
Can not find -sec LINUXCNC -var NML_FILE -num 1
Can